Putting on the Tune.
Author/s: Ray T. Bohacz
Issue: March, 2000

Optimizing The Ignition and Fuel System In An Older Engine

Even though the vehicle in this story is a '70 Vette with a 350, it is not about that. The voyage we are about to embark on is theoretical

and will be just as successful on any engine, regardless of make, number of cylinders, or displacement. All too-often, the participants in

this hobby fall into the replacement mode, not wanting to apply theory; switching components in lieu of tuning. Even after a pads swap in

most instances, there is horsepower locked away that can be finagled with a turn of a screw or the bending of the float. The first step is to

fully grasp what needs to be accomplished, and that is how the engine responds to spark advance, ignition, and fuel--the areas the we

can easily alter. Here, the lost art of tuning will be presented.

Air/Fuel Ratio

Some think that the more fuel you feed an engine, the higher its output will be. This is only a half-truth; an engine makes the most power

when there is a sufficient amount of fuel to burn all of the oxygen in the bore. If there is more fuel than oxygen to support it, or if the flame

extinguishes prematurely, leaving residual oxygen, the output of the engine diminishes. The old-fashioned method of tuning by reading the

spark plug color is not very accurate. The problem is that only extremes in mixture can be detected, since plug color is relatively

indifferent to slight changes in the air/fuel ratio. Modern technology provides more accurate, real-time methods of reading mixture utilizing

linear or wide-band air/fuel meters. These instruments can identify an actual ratio of fuel to air by measuring the oxygen content in the

exhaust with an oxygen sensor. These sensors differ from the ones used on production vehicles in that they can only accurately identify a

ratio of 14.7:1. Air/fuel ratio meters vary in acc uracy, with a price spread from $200 to over $10,000. It must be noted that any of the

current oxygen sensors will be degraded and eventually rendered inaccurate from exposure to leaded fuel. For our test session, we used

a custom meter that employs a Bosch extended-range four-wire sensor and ran the engine on 92-octane unleaded fuel. It is accurate to

two-tenths of an air/fuel ratio when exposed to a mixture richer than stoichiometric, or 14.7:1.

When we apply numbers, an engine requires the most fuel at peak torque and then needs to be leaned out at peak horse-power. The

volumetric efficiency of the engine is the highest at peak torque, since the bore is the fullest with charge, thus it requires the greatest

amount of fuel. Historically, most engines want an air/fuel ratio of 12.7:1 to 12.9:1 at peak torque, then lean out to 12.9:1 to 13.1:1 at the

power peak. Herein lies the importance of using an air/fuel-ratio meter, since an acceptable deviation is only 1.5 percent. Being a tuner

requires more than just reading a meter and shooting for a certain number. Fuel can also be used as a coolant, quenching the cylinder and

warding off detonation. In many instances, an experienced tuner may chose to run the mixture slightly rich, giving away a minute amount

of power, but then initiating a more aggressive spark advance curve due to the cooler combustion chamber. This logic often leads to a

positive power gain. Even with this technology, do not dismiss spa rk plug reading. It can be used for other diagnostic purposes. Mixture

variation from cylinder to cylinder and the beginnings of detonation can be verified with dose examination of a spark plug. Edelbrock

provided two different secondary metering rod combinations for our Q-Jet to allow altering of the air/fuel ratio. Our carburetor was

originally equipped with secondary metering rods BG while the Edelbrock rods were CE and CC, in theory, one step richer and leaner

than our base setting. ACCEL offers an oxygen sensor bung that we welded to the engine pipe exiting the exhaust manifold for

attachment of the air/fuel meter.



Continued from page 1

Ignition Output

With the popularity of nostalgia-based cars and engine compartments, it may be deemed undesirable to add an OE-style electronic

ignition to an early vehicle. This forces function to follow form, unless a little ingenuity is applied. We choose to incorporate ACCEL's

new 300+ digital CD ignition system and trigger it from the stock tach drive GM points distributor. The 300+ offers the latest in digital

electronics in lieu of slower responding analog controls while offering the power of an arc welder. Since the points will now be used only

as a trigger and will not carry any amperage, their life span will increase dramatically, only to be diminished from wear of the rubbing

block.

Switching from an inductance-based ignition system, which is what a points or factory HEI is to a capacitive-discharge design, offers

many benefits. The ACCEL ignition offers multistrike capability below 3,000 rpm and higher current and voltage outputs. The design

criteria for an ignition system is to supply the highest voltage and amperage for as long in the crankshaft's rotation as possible. This will

allow the most efficient conversion of fuel to energy. Ignition bum time is referenced in degrees of crankshaft rotation at engineering levels;

a layperson may be more familiar with milliseconds of arc duration. ACCEL has a companion epoxy core ignition coil, but we decided on

the cylindrical oil-filled Super Stock coil to retain the original mounting bracket and look.

Spark-plug gap is a concern; it is desirable to have the widest gap possible so that the ignition system can fire without degrading burn

time. Our subject 350 had older cylinder heads that required a short-reach 13/16-inch plug. With this ignition, it is beneficial to open the

plug gap to at least .040 inch on high-compression engines and to .050 inch on a street application. Our spark plug did not offer enough

side electrode length to go beyond the original setting of 0.035 inch, limiting the affect of the added output. A wide gap serves the

purpose of exposing a larger ionization window and increases the energy required to create a path to ground.

Spark Advance and Rate of Gain

In an engine, the piston travels faster than the flame expands across the bore. This necessitates giving the flame a head start, meaning that

it is initiated prior to the piston reaching top dead center. Start the flame too early and the cylinder pressure will start to rise while the

piston is still traveling toward TDC, creating abnormal combustion and decreasing engine output; too late, and peak cylinder pressure is

reached later in the crankshaft's arc of rotation, killing power and raising exhaust gas temperatures.

Simply put, anything that will affect the flame speed will determine the rate of spark advance that the engine will want to produce

maximum brake torque (MBT). Combustion chamber shape and design, spark plug location in relation to the bore center, mixture

motion, compression ratio and piston-crown design are only some of the considerations.

Continued from page 2

For ignition tuning, ACCEL supplied an adjustable vacuum advance and mechanical weight and spring kit. Using a dial-back timing light,

the spark advance curve would be documented.

Quantifying the Changes

Ida Automotive was enlisted to do the tuning and installation of the parts, as well as provide the use of their DynoJet chassis dyno.

Owner Bob Ida has years of experience extracting the most from any engine, and his facility is fully equipped with the necessary

equipment. As an authorized ACCEL EMIC, he is well-versed on not only ignition, but EFI systems as well. At press time, Ida was the

only facility on the East Coast with the new DynoJet friction brake. Prior to this option, as it is an inertia dyno, only wide-open throttle

tuning could be performed. This left the part-throttle functions of spark advance and mixture to be done seat-of-the-pants style. With the

friction mechanism, the engine could be loaded through the drive wheels, simulating various driving scenarios.

It must be noted that all results at the drive wheels are approximately 80 percent of the flywheel rating. This is the loss from the drivetrain

and volumetric efficiency changes that occur when the engine resides in the frame of the vehicle. When tuning an engine, the percent of

gain is what needs to be recognized more than the total power number. We all like to see big dyno numbers, but a tuner looks at the

delta, or change, in output. As an example, if an engine produced 100 hp at the drive wheels, and through tuning that figure was raised to

135 hp, at first it may not seem that impressive. Mathematically, though, that is a 35-percent gain in power without changing any hard

parts. In contrast, a 400hp engine tuned to 435 ponies is only a 9-percent gain.

The Real World

After a day of thrashing Jon Racich's beautiful Vette on the dyno, we made some interesting discoveries. For accuracy, each change was

verified by making multiple pulls and then accepting the repeatable results. Due to space constraints, we will represent the changes and

how they affected the engine, but in actuality we made 43 pulls in total. With all of that said, let's move into the chain of events and see

how we used our heads to tune for power.


RPM BASELINE ACCEL KIT
700 10 10
1,500 17 25
2,000 22.5 26.5
2,500 24 31
3,000 24 34
3,500 24 36
Final curve with vacuum advance
at part throttle, light load
RPM Total Advance
700 33.5
1,500 37
2,000 42


Even though we used the $2,000 linear air/fuel ratio meter (left) for our tuning session, it would be overkill for the enthusiast who wants to

tune his own engine. To meet the need for an inexpensive mixture analyzer, Edelbrock has brought to market its low-cost air/fuel monitor.

Working with an OE-style oxygen sensor, the kit comes complete with the appropriate bung to mount the sensor, wiring harness, plus

instructions, Instead of a digital readout with an actual ratio, the Edelbrock meter uses a series of 7 LEDs to indicate an approximate

mixture. This unit can be affixed to the dashboard with the supplied Velcro strips or be installed temporarily for tuning, being used as a

tool. No longer will you have to guess at carb jet sizing or how the weather is impacting air/fuel ratio.

Continued from page 3

Bob Ida documented the timing curve and found that the vacuum advance was not working, while the centrifugal advance was issuing

only 14 degrees, for a total spark lead of 24 degrees. The baseline dyno pull netted some disappointing numbers all around. Peak

horsepower was 169.7 and the torque came in at 235.9 lb-ft. Of greater concern, the engine was dangerously lean, with a wide-open

throtte (WOT) air/fuel ratio of 14.3:1. We needed to fatten it up before we added any spark advance. With this mixture ratio, the lack of

spark advance was what saved this engine from detonating.

To guarantee valid results, we installed new ACCEL ignition components, including the vacuum advance unit, and adjusted it with the

supplied 3/32-inch hex wrench. Tuned through the vacuum port, we seated the adjustment fully counter-clockwise as a starting point.

The unit was set using the dyno brake to provide a total timing curve of 42- degrees BTDC. This provided the best throttle response

without getting detonation. Since there is no vacuum signal present at WOT, it would not affect this part of the test.

Edelbrock supplied the two choices for secondary enrichment, one step richer and leaner than we already had. After installing a set of

smaller-diameter Edelbrock metering rods, we made another dyno pull, concerned only with mixture and found the same problem --

14.3:1 air/fuel ratio, no change at all. Since the engine had a new fuel pump and filter, we decided that the fuel supply problem had to be

in the float bowl. After removing the air horn, we discovered that the float level was 3/32-inch too low. The richer metering rods could do

nothing if we were running the bowl out of fuel. We raised the float level 1/32-inch above specification and readjusted the secondary air

valve tension, since it was too slow to respond. We were rewarded with a reading of 12.7:1 at peak torque and 12.9:1 at peak power.

The dyno readings were up 6 hp and 7 lb-ft of torque.

We went back inside the distributor for a weight and spring change. Before we installed any new parts, we sprayed brake cleaner on the

breaker plate, checked its movement, and lubricated the slides with a high-temperature grease. The ACCEL kit offers three spring

choices; we choose the blue medium-tension one, which in theory should give full advance by 2,800 rpm. On the chart, the advance rate

for the three spring choices is referenced in distributor rpm, which is one-half the crankshaft speed. ACCEL also includes a new travel

stop, but we wanted to check the timing curve with the changes we had already made. But, we were wrong; it didn't work. We still had

the same total advance, it just came in sooner. The distributor would have to come out and the shaft removed to install the new stop.

It didn't take long to find the problem; someone had added a braze to the stop, making it thicker and limiting the travel of the advance

mechanism. American ingenuity took hold and Bob Ida filed down the braze to a dimension small enough to accept the ACCEL bushing.

We now had 36 degrees of total advance and found 23 hp and 22 lb-ft of torque! An ignition coil has no moving parts, but it does wear

from being charged and discharged. To be complete, we also swapped to a new ACCEL Super Stock coil and gained 5 more ponies

and 5 lb-ft of twist.

Continued from page 4

Car owner Jon Racich found the perfect hiding place for the 300+ box, in the right-hand kick panel where an optional factory speaker

would have resided. Remember, when installing the ACCEL 300+ on a GM points ignition, the resistance wire from the starter needs to

be removed to provide full charging voltage to the primary circuit. With the new ignition connected, some interesting things happened.

The air/fuel ratio went rich, down to 11.9:1 and 12.2:1, respectively we lost power. This indicated that the 300+ was working, burning

fuel that we were wasting before. The engine was now too rich with our original choice of metering rods. Ironically, these same rods

provided the proper mixture ratio with the weaker ignition. We swapped in the other set of Edelbrock metering rods, brought the air/fuel

ratio back up to 12.9:1 and 13.2:1, and found 7 hp and 5 lb-ft.

As a final touch, we added the high-flow ACCEL washable air filter element and came away 3hp and 3 lb-ft.

Master tuner Bob Ida is pleased with the results. He found 44 hp and 42 lb-ft of additional torque for totals of 213.7 and 277.9 for

torque and horsepower respectively. Other than the ACCEL ignition and air filter, the engine is the same as when it rolled in. Fuel

mileage, throttle response and idle quality have all improved.